The Sankeshu Locomotive Depot carried out the "Encircle the fighter plane to break the XNUMX-day breakthrough" activity

Time: 2018-04-15 Browse:
Recently, the Sankeshu Locomotive Depot launched a hundred-day "Encircle the fighter plane and break the 4-day research" activity. During the research process, the cadres and employees worked together on the locomotive and formed a research team to overcome difficulties and find out. The real culprit of the "intractable diseases" of locomotives.This event specially selected dispatchers and work team leaders with extensive maintenance experience to form a research team.Regarding the various "difficult and miscellaneous diseases" that have appeared in locomotives, it is emphasized that the ones that can be repaired cannot be replaced, and the ones that cannot be repaired must be developed to tackle key problems.At the end of last month, the DF0142D No. 14 locomotive experienced fuel injection from the turbocharger chimney.This phenomenon still exists after the cylinder head is pulled out, the injector is changed, and the high-pressure oil pump is removed.According to past experience, replacing the supercharger is the "best policy", it is not bothersome and "safe".However, the research team did not adopt this method, but wanted to show the "true culprit".After repeated analysis, demonstration, and investigation.A small amount of oil was found on the cylinder block of the diesel engine's 11th cylinder. After thorough investigation, it was found that a piston pin in the cylinder had fallen off.After replacing the piston pin, the "fuel injection symptom" is eliminated. At the beginning of November, DF4D No. 3321 locomotive had abnormal sound of the front gearbox. After the gearbox spindle was covered and checked according to the process, the gap of the spindle shaft was adjusted continuously and the cardan shaft was replaced. The gearbox was abnormal. The sound has not been eliminated.After two consecutive days and one night, the research team sorted out, analyzed and checked the fault phenomenon again and decided to conduct on-vehicle disassembly inspection of the gearbox.After two consecutive days of technical research, it was finally found that the abnormal sound of the gearbox was caused by the falling off of the exciter shaft oil seal oil sling pan.It is reported that since the launch of this activity, the Sankeshu Locomotive Depot has discovered and eliminated nearly ten hidden quality hazards of locomotives, which has greatly promoted the enthusiasm of cadres and employees for careful inspection and repair, and the enthusiasm for winning the winter sports and the overall improvement of vehicle repair skills. . (Shi Hongyan)